Erik,
Just a thought. The 7805 in your schematic appears to be a big part of
the signal chain. I've run into issues with 78xx series regulators being
noisy. Spent a few weeks chasing down noise issues in some equipment and
the 78xx regulator was a part of the problem. Replaced it with LT3042 as
part of the solution.
Also note, not all 7805's are created equal. Different vendors may be
better/worse than others.
Good luck!
Dan
On 7/12/2022 9:45 PM, time-nuts-request@lists.febo.com wrote:
I'm struggling with the noise floor.
First tests where done with a 5nV/sqrt(Hz) opamp. Noise floor with
shorted mixer output at 10kHz was -140dBc/Hz. Then I tried with
1nV/sqrt(Hz) opamp, but that made no difference, noise floor at 10kHz
was still -140dBc/Hz
The setup was simplified to this schematic:
http://athome.kaashoek.com/time-nuts/PNA/SSPNA.JPG
The REF_buffer creates a virtual ground, the Audio_LNA amplifies into
the differential audio output .
Why did the lower noise opamp not make a difference?
Also the setup is acting like a nice microphone. Tapping the housing is
clearly audible. Which component may be causing the microphony?
On 7/13/22 5:24 AM, Dan Kemppainen via time-nuts wrote:
Erik,
Just a thought. The 7805 in your schematic appears to be a big part of
the signal chain. I've run into issues with 78xx series regulators
being noisy. Spent a few weeks chasing down noise issues in some
equipment and the 78xx regulator was a part of the problem. Replaced
it with LT3042 as part of the solution.
Also note, not all 7805's are created equal. Different vendors may be
better/worse than others.
Good luck!
Dan
+1 for the 200 mA LT3042 (and the higher current 0.5A LT3045). There are
now negative voltage versions, too, LT3094, also 0.5A.
Noise from 10Hz to 100kHz is around 0.8 microvolts. At 10 kHz 2
nV/sqrt(Hz). But the real thing these things are good at is PSRR at
higher frequencies. >70dB at 1 MHz
They have enable inputs, can be paralleled willy-nilly, etc
On 7/12/2022 9:45 PM, time-nuts-request@lists.febo.com wrote:
I'm struggling with the noise floor.
First tests where done with a 5nV/sqrt(Hz) opamp. Noise floor with
shorted mixer output at 10kHz was -140dBc/Hz. Then I tried with
1nV/sqrt(Hz) opamp, but that made no difference, noise floor at 10kHz
was still -140dBc/Hz
The setup was simplified to this schematic:
http://athome.kaashoek.com/time-nuts/PNA/SSPNA.JPG
The REF_buffer creates a virtual ground, the Audio_LNA amplifies into
the differential audio output .
Why did the lower noise opamp not make a difference?
Also the setup is acting like a nice microphone. Tapping the housing
is clearly audible. Which component may be causing the microphony?
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Am 2022-07-13 15:50, schrieb Lux, Jim via time-nuts:
On 7/13/22 5:24 AM, Dan Kemppainen via time-nuts wrote:
Just a thought. The 7805 in your schematic appears to be a big part of
the signal chain. I've run into issues with 78xx series regulators
being noisy. Spent a few weeks chasing down noise issues in some
equipment and the 78xx regulator was a part of the problem. Replaced
it with LT3042 as part of the solution.
Also note, not all 7805's are created equal. Different vendors may be
better/worse than others.
+1 for the 200 mA LT3042 (and the higher current 0.5A LT3045). There
are now negative voltage versions, too, LT3094, also 0.5A.
Noise from 10Hz to 100kHz is around 0.8 microvolts. At 10 kHz 2
nV/sqrt(Hz). But the real thing these things are good at is PSRR at
higher frequencies. >70dB at 1 MHz
They have enable inputs, can be paralleled willy-nilly, etc
I have measured the noise density of an assortment of regulators
under the same conditions and in the proposed circuits of their
data sheets. I don't believe in different brands of 7805; they are
all ugly.
<
https://www.flickr.com/photos/137684711@N07/24070698809/in/album-72157662535945536/
You can increase Cset on the 3042 to 100u tantalum. That helps at the
low
frequency corner. More does not help. For the output capacitor, 4u7 is
optimum. More produces a noise peak at 100 KHz or so.
The trace of the 3042 is sandbagged at the low end because of the input
capacitor issue with my then-preamp I explained a few days ago.
Paralleling lt304* is not cheap, althoug it drives the noise further
down.
The circuit from the data sheet with the external NPN is about as good
as
a single 3042. I tested it with 1.5A. It takes a little bit more input
voltage, abt 6V4 for 5V out, but is cheaper than many LT304* in
parallel.
Gerhard